Improvements in the Design of the Cyclohexane Production Process Implementing Mass Exchange with a Counter Current Gas Permeation Membrane
Industrial & Engineering Chemistry Research2012Vol. 52(4), pp. 1698–1704
Citations Over TimeTop 16% of 2012 papers
Abstract
In this paper, we propose changes in the design of a cyclohexane production process, following a mass exchange design heuristic developed in a previous work (Ind. Eng. Chem. Res.2011, 50 (11), 6849–6859). In the study case considered, an optimal design was obtained which exhibits a significant 40.08% reduction in the power of the compressor that recycles unreacted reagents, and a respectable 3.59% reduction of the hydrogen consumption, resulting in an increase of the plant Net Annual Income of a 1.31%. These results highlight the importance of considering a mass exchange between the input and output streams from the reactor, at the time of synthesizing a new process.
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